This gas injector/producer well was drilled in 2014 to a depth of 2635 mAH. After the well was completed and tested, coiled tubing was used to retrieve a 5.75” RPT standing valve installed in the packer tailpipe. Pressure differential over the valve was equalized using nitrogen. Coiled tubing was not able to free the valve. Two CT BHA’s were left behind in the well.
The objective was to mobilize the snubbing unit and to fish the lost CT fishing BHA which lay on top of the original CT BHA which was still connected to the 5.75” RPT standing valve.