This gas injector/producer well was drilled in 2014 to a depth of 2635 mAH. After the well was completed and tested, coiled tubing was used to retrieve a 5.75” RPT standing valve installed in the packer tailpipe. Pressure differential over the valve was equalized using nitrogen. Coiled tubing was not able to free the valve. […]
The well was drilled in 2012 to a depth of 2635m AH and was found dry. The 13-3/8” and 9-5/8” casing-shoes were set at 564m and 1295m respectively. The well was permanently abandoned by means of 5 cement plugs. The 9-5/8” production casing was cut and retrieved from 600m creating a uncased hole section of […]